Por favor, use este identificador para citar o enlazar este ítem: http://dspace.udla.edu.ec/handle/33000/12119
Tipo de material : bachelorThesis
Título : Propuesta de un modelo de mejora continua de los procesos en el área de producción de una metalmecanica aplicando herramientas Lean
Autor : Cevallos Maldonado, Manuel Fernando
Tutor : Chicaiza Salgado, Edison Rubén
Palabras clave : INDUSTRIA METALMECÁNICA;CONTROL DE PROCESOS;PRODUCCIÓN INDUSTRIAL;OPTIMIZACIÓN INDUSTRIAL;HERRAMIENTAS LEAN
Fecha de publicación : 2020
Editorial : Quito: Universidad de las Américas, 2020
Citación : Cevallos, M. (2020). Propuesta de un modelo de mejora continua de los procesos en el área de producción de una metalmecanica aplicando herramientas Lean (Tesis de pregrado). Universidad de las Américas, Quito.
Resumen : El presente proyecto de titulación se enfoca principalmente en la eliminación de piezas defectuosas durante la fabricación de chasis en una empresa ecuatoriana metalmecánica…
Descripción : This project is focused mainly on the elimination of defective parts during the chassis manufacturing in an Ecuadorian metalworking company. A study of processes within manufacturing areas was carried out, processes that involve the elaboration of parts for chassis assembly, with this study the parts were identified where more percentage of defects were found in order to attack the. In addition, a SIPOC diagram and flowchart were made, allowing to understand the processes and activities of each piece more thoroughly. Once de main defects have been identified and each process has been thoroughly understood, there were used an Ishikawa diagram to find the root cause of the problems. It was analyzed and identified the most optimal Lean Tools to apply and those that would bring better results, in this case they are: 5 S, which allowed to have a better managed order, cleanliness and standardization within the company, another tool that was used was the TPM tool that helped improve the availability of time within the organization, SMED also provided assistance at the same point allowing a more optimal handling of the transfer of dies and finally the use of Poka Yoke that allowed the defects of missing perforations and displaced perforations are solved, significantly reducing the percentage of defective parts within the production area. As a result, an increase in the OEE in the manufacturing area was obtained, due to the improvement in the availability of time, machinery efficiency, and defective parts reductions, as well as significant economic saving due to the lower amount of raw material discarded, achieving savings for the company of 3,582.70 dollars per month.
URI : http://dspace.udla.edu.ec/handle/33000/12119
Aparece en las colecciones: Ingeniería en Producción Industrial

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